B2
B1

The Demon Returns by John Whetton.
A Sequel to "All Fired Up ready for Silverstone".

I thought the problem with the flooding carburettor and the consequent and damaging fire to GDP 38 was an experience now confined to history. Sadly, this has not been the case, but fortunately I have no further fires to report.

The flooding problem had gone the day after the fire, the car drove perfectly up to the paintworks man in Chesterfield and back a few days later. A few trips out in the car appeared to have proved the point that the disaster was behind me. A week later, a cold start resulted in the same problem; gushing petrol fumes from the exhaust pipe. Since the symptoms cleared themselves after the day of the disaster, I concluded that it would do so on this particular day and so I took the car out for a good drive in the hope that loads of accelerator would clear the beast's throat. After 20 minutes the poor car failed to proceed at a traffic light and with a high degree of embarrassment I had to be pushed to prevent a major traffic jam. A considerable amount of fuel had been consumed in that short journey and having removed the spark plugs to hack off the soot, the car did fire up with some reluctance and then it drove like a dream for the rest of my journey. This state of compliance on the part of the carburettor prevailed for a further week and a number of one to two hour pleasure trips. Sorted once more and hopefully for good, I thought.

Defiance Prevails, Headaches Develop
Come the weekend of July 15th, The Demon returned. My frustration is difficult to put into words. I needed help. Based on my understanding of the problem, centreing around the needle jet in the float chamber, a call to Fiennes restoration resulted in a new jet and seating to replace the suspect pair I installed just 18 months ago. The parts were with me within 24 hours and Jason Fox came down from Chesterfield to investigate the matter. The new components were installed and the seal was perfect. I fired up the engine, but the problem persisted. The carburettor was removed from the engine for further examination. Was it the ventura, the slow speed jet or the high speed jet? These seemed to be in good condition following Jason's rebuild of the carburettor some time ago and so the unit was reinstalled on to the engine. I fired her up again, but no change was evident.

It was by now almost bed time. We knew that the carburettor on GAU 15 was a fine affair and so a decision to remove it and install it on to GDP 38 was made. It was with tears in our eyes that we yet again witnessed the high levels of fuel in the exhaust output. We called it a day. We could both sleep on the problem (not that I could sleep with such a matter in my mind) and come to some sort of rational conclusion the following morning. Essentially, the true problem lay not with the carburettor but something which either controlled it i.e. rods and levers or something else. It suddenly dawned upon me that the excess fuel in the exhaust was not even passing through the carburettor but straight into the cylinders via the inlet manifold. The culprit had to be the Autovac. Over the telephone, Jason agreed and gave me some instructions for further investigation.

Carburettor: Not Guilty
If the current suspicion was that the Autovac was flooding fuel directly into the inlet manifold, a tell tale sign would be the union between the Autovac vacuum pipe and the manifold. On loosening this, the evidence was in fact there; petrol was dripping from it. I then removed the brass head to the Autovac. As I was undoing the cheesehead bolts which seal and secure it, I could hear the gurgling of fuel from the upper to lower chamber as the airtight seal was being broken and on removing the head with its attached float and sprung-loaded closing valve, everything fell into sharp focus. The float slurped with petrol within. The float had been 'waterlogged' or rather 'petrollogged' and was therefore less of a floater, more of a sinker! In consequence it was incapable of rising sufficiently within the cylinder to close off the inflow valve and as soon as the engine was doing its job, the suction force generated by the inlet manifold was drawing uncontrolled amounts of fuel into the upper chamber, filling it with the consequential inevitability of the stuff pouring down the vacuum pipe, thus overwhelming the manifold and then the six cylinders with a dire result.

On close inspection of the Autovac float, it was clear that the bottom solder seam was perforated and in a suitably angled position it drained of its internal fluid within 20 minutes. These new facts were reported to Jason who had a quiet sigh of relief over the telephone. He suggested a call to Autovac Spares of Moulton, near Northampton to ascertain if they could help and within 24 hours, thanks to Michael Wyndham-Grice, the company owner there, I had a replacement float. I quickly opened the parcel, switched the two floats and within two minutes the Autovac head and unions were secure. There was then a few minutes of suspense and a cup of tea. With some degree of intrepidation, I turned on the fuel tap, set the quadrant controls and fired up the engine. Bingo !...No cloud of petrol gushing from the exhaust tail-pipe and although running a bit on the rich side, the problem appeared to be overcome. The spark plugs were removed and the soot brushed off and an evening out with the hood down to the lovely village of Crich in Derbyshire (the home of The National Tramway Museum) to meet up with section members for our annual visit to the fish and chips restaurant there (The Cardale Fish Restaurant in the TV series, "Peak Practice"). What a story to tell !

Closer Inspection For Other Matters.
Within a few days, the Autovac head was off again for a visit to Autovac Spares for Michael to replace the petrol inlet valve and to conduct a general overhaul of the system, replacing parts as necessary. I had been suffering for two years or more from a frustration caused by what appeared to be fuel starvation manifesting itself as 'kangaroo' power losses and surges, lasting perhaps 30 seconds, not only on hot days but also during the winter. I never resorted to the aluminium foil 'remedy' because I have little faith in it. I assumed an Autovac problem but more associated with the old float possibly catching and sticking at an angle on the cylinder sides. On removing the float, it seemed clear that the soft solder seam had been poorly repaired at some point in the past and was very rough. Perhaps this was causing friction, thus preventing free excursion of the float. Using a carefully administered fine file followed by lapping paste, I smoothed out most of the offending protuberances. With hindsight now, I believe I had rubbed down on a particularly thin area of solder and created that fine perforation responsible for the less than buoyant float described above.

A Retrospective Analysis
How did the petrol find its way into the float? The perforation was minute to say the least, but with rises in temperature, both climatic and engine-induced, expanding air would have been forced out of the float and liquid petrol sucked in later as the Autovac and ambient air cooled. This slow process would have been a creeping affair over a period of many weeks until a critical mass of fuel in there rendered the float incapable of ascending high enough to shut off the valve on the one hand and on the other descending too far, too early, possibly restricting the gravity-fed flow into the lower chamber.

Why the flooding carburettor? In my opinion, the fuel vapour/air mixture generated by the carburettor passing into the inlet manifold system would have been meeting an overwhelming force of liquid petrol now evaporating partially and expanding rapidly on account of a rising engine temperature and preventing free flow of the carburetion mixture, so much so that I can only think of the analogy of the force of a Tsunami. It is therefore likely that the carburetion mix was being forced back whence it came and the pressure thus created preventing further activity of the carburettor.

The Autovac: Another Moving Part for Regular Maintenance.
One thing I did learn from my visit to Michael Wyndham-Grice's workshop in Moulton is that the Autovac is yet another item of engine support that must be inspected and parts replaced every couple of years or so. It might be prudent for members to remove the Autovac head and send the thing, complete with float, to Michael for him to cast his eye over it, strip it down and get it up to scratch.

Michael was most helpful and generous in his dealings with me. I can recommend him to all enthusiasts with cars reliant on an Auotovac. He has a good stock of replacement parts.

Michael's address and telephone are as follows:
36, Oundle Drive
Moulton,
Northamptonshire,
UK
NN3 7DB

Tel: 01604 647181